The captain of a Beechcraft 390 Premier failed to follow the correct procedures for an anti-skid failure, resulting in a fiery crash
that killed five passengers, the NTSB said in its final report on
Tuesday. The jet was returning to Thomson-McDuffie County Airport, in
Thomson, Georgia, on February 20, 2013, when it failed to slow down
after touchdown. The captain initiated a go-around. Nine seconds later,
the jet collided with a utility pole about 1,835 feet from the end of
the runway, 63 feet above the ground. The captain and first officer
suffered serious injuries. NTSB Acting Chairman Christopher Hart said
crew fatigue was a factor in the accident.
"This pilot's inadequate knowledge of his aircraft was compounded by
his fatigue," said Hart. "As a result, five people died who did not have
to. Just as pilots should not take off without enough fuel, they should
not operate an aircraft without enough rest." The captain failed to
adhere to the airplane's flight manual procedures for anti-skid failure
in flight and did not retract the lift dump -- a critical system to
assist in stopping the aircraft -- immediately after making the decision
to perform a go-around, according to the NTSB. According to the
checklist for an anti-skid system failure, the flap configurations
available for the pilot were flaps up or flaps 10. Either of these
configurations would have required a longer landing distance than the
runway provided. As a result, the pilot should have sought landing at an
alternate airport, the NTSB said.
Investigators found the aircraft had extended flaps 30 on the
approach, which is prohibited by the anti-skid failure procedures. At
the time of impact, the flaps were transitioning through flaps 15.
Additionally, while both the airplane's flight manual and a placard in
the cockpit warned against extending the lift dump in flight, the
go-around was attempted with the lift dump deployed, making a safe climb
unlikely. The full report is posted online.
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